My goal is to have the Merc run as good or better than new and as I dug into the old motor deeper I went from frustrated with the mess to determined. I was intimidated by the wiring strung seemingly all over on the motor but now after removing every terminal and wire, I see it as being super simple as my mind can now connect every last wire on the motor.
- wired in new switch boxes.
- new coil on #1
- rectifier replaced
- flywheel removed stator out (trigger wires look just fine, I'm surprised but think it may have been replaced at one point)
- internal wiring harness removed
Waiting on stator, harness and ign switch to arrive.
The LW, I would essentially have what I have now with the standpipe if I plumbed the new overflow drain into the same line. My resto buddies Smokercraft is set up with an overflow out the side and the drain goes out the stern. My SN is set up with the overflow and drain T'd into one drain but the livewells are different in height, size and position in the boat not too mention aren't sealed tight.
- got my spare 1-1/8" thru the hull fitting in the LW. (always have an extra in stock)
Waiting on 2 more fittings to arrive and the 1-1/8" LW drain hose.