Next up, with the engine back in the boat was time to align the engine to the drive shaft.
This I was a little nervous about since all the mounts were pretty old, so last week (maybe 2 weeks ago
:blue
I took them apart and cleaned up the oxidization and got all the adjustments working the way they should. WHAT A GOOD IDEA. It wasnt too difficult to move the engine and mounts around... but I cant imagine what effort it would have taken if the adjustments and slides were seized.
Lowering the engine onto the angle iron was easy enough, although again, wish I had the chain hoist. from there I adjusted the straps on the engine so that it would pick up almost square, and then put a little pressure on the strap. This allowed for easier moving of the engine.
I had a 4' 3x3 board that became my pry bar. Being sure to ONLY pry on parts of the engine, mounts, or stringers. There is a lot of cabling, hoses, wire, or thin sheet metal that would have certainly bend/broken. I did this to get the engine mounts mated up to the angle iron as best I could, and then clamped them to the stringers so that they would somewhat stay in place.
I did the best I could to eyeball the side to side alignment of the engine to the shaft. Pulling that coupling up to meet the engine/trans helped to see if I needed to rotate one way or another, etc. On my mounts there were slides which are locked into place with a bolt that has a half moon cut out of them. They fit into the "slide" hole and when tightened, will bite onto the shaft that is your side to side adjust. with the mounts fixed, i pried the engine block back and forth until the alignment was straight-ish.
After the engine was square to the drive shaft I started adjusting the height of the mounts to have the angle of the engine match that of the shaft. This was done with the rear mounts by rotating the center threaded rod to have the mount piece with threads on it move up and down. This was a pretty simple adjustment. Once it was in a good spot I tightened the Jam nut on top down and tightened up the side/side slides.
few tweaks here and there and I got the engine shaft within 0.005" with my feeler gauge. I want to say that 8 thousandths is what I read as the good limit. So I'm happy with it.