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- Jul 23, 2011
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If spraying with water causes it to run bad, start with dielectric grease in the plug wire boots.
Water mist shouldn't cause it to run bad
Water mist shouldn't cause it to run bad
Replace the wire from coil to cap the archng is loosing sparkOF course I couldn't duplicate on the trailer in the dark... So no go there. I lightly misted down the coil with water from a spray bottle... Caused it to run like sh!t and stall several times. Couldn't see any visible arcing. Monday is another day, got 3 days of work for the time being.
I did add a little when I replaced the plug wires with the cap last week, but I can repack and check again. The coil had a heavy residual from the old wire I cleaned out. It was such a small mist too that it caught me off guard... I could see if it got hosed down but I'm talking like 2-3 mists from a water spray bottle.If spraying with water causes it to run bad, start with dielectric grease in the plug wire boots.
Water mist shouldn't cause it to run bad
I double checked all the wires last night after it started acting up. I plan to repack the ends with some dielectric when I get the chance. I am hesitant to replace the coil only because I can count of two instances where the coil was actually the problem... for the most part when I've delt with them, they either work or they don't and I'd rather not just start throwing parts at it. It needed plugs/wires/cap and rotor regardless so that doesn't hurt but I'd rather take the time and actually diagnose the problem and or just fix things that are problems as I find them... see below.Reacting on water is indeed not good. I would start to check the spark cables for a good connection. Especially the one from the coil. Or replacing the coil. The rattling should be gone. You where also talking about a leak in the intake gasket. When a engine is warm the gap can extend. If there is air coming in through that gap the mixture will change (lean) this also can cause back firing/popping in the carb.
It followed it from the old wire set to the new one.Replace the wire from coil to cap the archng is loosing spark
This is odd - is the top of the coil cracked? Only things I could think of is its coming out of the coil top, the wiring harness is too close and its jumping from HT wire, or you dont have a great cap to rotor connection and the spark has no where to go- only time I saw this was disconnected by coil wire off cap to spin engine without ignition and didnt have the cap end grounded. Made similar arcing to what you are seeing. was arching under boot on coil to one of the coil terminals...It followed it from the old wire set to the new one.
My guess is timing off when running cheap gas.Problem is different enough that rather than cluttering up my carb thread I figured it best to start a new thread.
So what happened: Ran the boat today after rebuilding the carb. Ran for about 2.5 hours with an hour break in the middle. So out on the water for 3.5 hours total. Upon nearing the ramp I started pushing it a little... nothing crazy, 3600 rpms for maybe a minute or two. Got a single pop through the carb under the spark arrestor. So I backed off to 2800 to investigate. It didn't sound quite right, but wasn't missing. Dad cracked open the dog house and all of a sudden it popped several times like pop corn. I dumped the throttle and idled it the 1/4 mile to the ramp. Seemed fine but I wasn't going to try pushing it any harder.
So when I got home I checked a couple things, pulled the plugs to make sure nothing looked scary, and they're good. No detonation, timing mark on the strap is good, fuel mixture seems about right. Nothing to write home about.
So next I ran a compression test, saw about 160 across the board, so again, nothing abnormal.
Finally I pulled the cap and rotor. Seems like a little scale build up inside and there were these points, not corrosion but a little slag hanging off the tip of one of the electrodes. I plan to pick up a cap and rotor tomorrow as well as plug wires.
I think that is a good place to start. I also have had issues in trucks in the past with the vortec style intake having vacuum leaks... but I wouldn't think it would run so well for so long then all of a sudden mess up. This happened a couple weeks ago too at nearly the same point in the trip... So there is that. I'm not denying that I messed up the carb but... I don't think it would run as well as it did if there were something wrong with what I did... but I am also an idiot and have been wrong many times before.
I'm just looking for input on if this is a good direction to move in for now. Appreciate it.
-Paul
I've checked out the choke while running... it comes off completely within 30 seconds of starting... 95 degree ambient temps plus 85 degree water temps, doesn't come on very long. I had tried the choke before I rebuilt the carb and all it did was bog it out by going pig rich... black smoke and all. I could try again another night.The ticking noise is now gone? If you're sure of a leaking gasket then change it. If the intake is leaking it can also cause back firing. When it warms up the gap can get bigger and if the choke is working it's getting more fuel when the engine is cold. When the engine heats up choke is coming of(more air) and it leans out. Are you sure it's getting enough fuel when the symptoms are coming up? If it's possible;try to close the choke when the problems are there. When it runs fine you know it's leaning out.
Most of my friends have substantially newer boats with delco EST and MPI or very old stuff with points still. The points coil may work, but from my understanding the thunderbolt coils are a little different. I could ask my friend at the marina, they are gutting some late 80s small block boats, I may find a serviceable one there.I read that's a clean dropout. If it looks like you switching off the ignition (like a cut out) then most likely it's in your ignition system. You are also talking about the temperature. It only appears after warming up. When the engine is running move your cables a bit. Also the connection between engine and wiring harness. Also check the switch interrupter if it works(not loosen) Specially when temperature is involved I would search around the engine (hottest place) not possible to swap the ignition coil for an other one (another boater)?
you must have milkshake for oil. did you do a compression test before tearing it down? Wonder if the pop is a vlave hanging up and backfiringWell, this isn't pleasant.
View attachment 384923
Alleged fresh rebuild from the guy I bought it from. I had the pan off right before I installed it, from the bottom, everything looked brand new... one of the lobes has pitting... I'm kind of disgusted right now.This one has leaked for a while... If it's possible try to check also the inside of the engine/pistons. That it was running...
Oil was clean both times I changed it... Ran maybe 9 hours before yesterdays outing which was the first after the change.... both look clean. Compression test when this started happening was 160 across the board.you must have milkshake for oil. did you do a compression test before tearing it down? Wonder if the pop is a vlave hanging up and backfiring
I have no idea. It was a "fresh rebuilt, low hour and ready to go" engine I purchased early may. Obviously, based on the fact I've had all of 5 hours put on the thing, I don't believe that to be entirely correct information. I can say I know of someone who won't be getting my business again... but at this point it's a pull and rebuild as that metal from the cam went through everything and the lifters are all going to be junk. I can't tell where it's coming from... but I suspect it's more than just an intake gasket leak.Is that all from the intake gaskets? Mine blew the head gaskets 2 years after an overheat but it didn't look that bad, even though it was in salt water. Judging by the rust in the intake ports it is possible an intake valve could be hanging open. When I pulled out all the lifters the cam looked like new. One thing I like better about the pre-Vortec engines, the intake gaskets rarely if ever leak.View attachment 384963