It has been a productive couple of months. I dug the boat out of the garage, hooked up the hose, and fired her up. Click, then, nothing. Well, thats not good. I have read enough on this forums to know that the answer of what to check is in the stickies. I check the slave solenoid, it is not functioning properly. The ignition swich is working, and the neutral safety switch works. Time to replace the solenoid. It goes in, and turn the key to see if it wanted to turn over. Success!
While under the dash, I also rewired the ignition switch. Someone had wired it up to the blower switch as well. (There was no blower in the boat, which has been corrected.) I could pull the key out of the ignition, and the boat kept running until the switch was also turned off. This has also been fixed.
Last week, got the boatbon the hose again, and tried to start. One click, then all the gauges die. Tried jumper cables to the truck, and she starts! Must need to throw the battery back on the charger. Which was weird, because it was sitting in the boat without the positive lead hooked up.
After a week on the charger, it still shows it is trying to charge. Back in the boat, same. A single click, and the gauges go dark. Maybe a bad battery? Take it to the store for testing. The girl can't get the machine to read properly, and says the 2 year old battery is bad. Still covered under the limited warranty, so the new is about half off. Works for me.
New battery back in the boat. Same issue. Start looking at the battery cables, and decide it is time to replace the positive. New cable goes in, and victory is mine! Boat is sitting in the driveway on the hose, running under its own power.
While all this is going on, realize that the shift cable bellows needs replaced. That is likely where the water was coming from last year. It was all cracked and dried out. Thankfully, I was able to get it replaced without pulling the drive. The admiral would have had a stroke if I started tearing into that right now.
On Sunday, with everything running, it was time for a lake test! Had to stop 3 times on the 20 mile drive to re-secure the new engine hatches, then the cover for the bimini. Get her backed down the ramp, and she fires right up! Good sign. Open the hatch: no water in the bilge. Good sign. The new steering system works like a dream. Feels like a brand new boat!
Got her on plane, and cruised the lake for a few minutes. All the gauges were reading as they should. Opened it all the way up. WOT is low, about 3400. Never tried it before the rebuild, as I had the whole family out. May need to look into that.
Throttled down, and started getting into a no wake zone. After a few minutes, I glance at the temp gauge. It is reading hot, and climbing. Not good. I turn around, and head to the ramp, watching the gauge. Once I throttle up, the temp drops to normal. Has to be the impeller going bad. Curious, I drop back to no wake speed, and temp starts going up again. I give it a little more juice, and we drop back down. The touch of throttle keeps me at no wake, and brings the temp to normal. I'll keep an eye on it the rest of the season, and replace this winter.
Back at the ramp, pulled the plug, no water came out! That made me smile. Overall, I would say it was a successful weekend. There is still some upholstey work to finish, but we are oficially spalshed! We are good to go for vacation next month. I can sleep a little easier tonight.