Two things: First, I took the boat out today on Monroe Lake... more on that later.
Second, since it seems that the photo issue isn't getting resolved any time soon, I've uploaded some things to Imgur... here's what I had worked on previously with some additional commentary based on how today went:
Internal Bilge Plug:
There's supposed to be a bilge plug there, which I did eventually find in a rusted solid state. Fixed with a new plug and a fresh chain:
No issues here... ski locker stayed nice and dry (yes, it was in the hole, not as shown).
New bilge pump: Here's the new power tap I added for the automatic part of the pump:
Eventually I'm thinking of redoing it by using a switch similar to the nav light switch with a 3rd middle position that only powers and using that for the "automatic" power feed for the pump. That way I can isolate the pump when driving/dry storing without needing to necessarily disconnect the battery. If I can even find a matching switch that doesn't stick out like a sore thumb. But for now, what's there works...
New bilge pump connections:
Yes that is 16-3 extension cord cable... but the old pump also used such for its power lead (black instead of orange, but orange is what I had a bunch of in my wire drawer). Note that I kept the original connector so I didn't have to modify any existing wiring.
Can't say that we saw the pump automatically kick on (being a "dumb" pump with a float switch, it does backfeed the manual wire which lights the console light), but there wasn't much water back there when the outing was over, so all is well. I think a lot of the water that came on last time was in fact a ton that was trapped in the tube canvas that accidentally drained into the bilge We did tube a bit today, but it was a with a different tube that didn't have that issue.
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Had a couple issues. First, for the second time, the steering wheel hub cover popped out on me. Since the wheel hub is cracked, I'll probably replace the wheel if I can (seems to be a standard tapered shaft + keyed type wheel, universal?)
Second issue probably ended the season though... the captain's chair busted on us.
Been making some bad noises, but had no idea it was this bad... also didn't know this cushion had a wingnut that was supposed to allow it to be removed to reveal a bit more storage:
The cover has a small hole too. The rear cushion needs new foam/upholstery (animal damage present when I got the boat)... and the back of said chair has a small tear (on par with the side upholstery). That said, the small damage I can't be bothered about (as this is a boat in use, not a show/museum piece)... but obviously I need a new seat board for the captain's chair and will get the rear seat cushion redone (good original board, has been reupholstered once before). Not sure if the board is something I should make myself (my FIL has a wood shop, probably could make pretty easily with a router using the busted one as a flush bit template)?
Also of note is that
I did determine WOT on this thing is 4050RPM and 41-42MPH on the current prop. Not the "over 50MPH" that the boat was advertised as, but that was with a very different prop (Aluminum Mercruiser 14.25"x21Px3, currently I have a composite piranha 14"x18x4) ... hole shot not very good on the stock prop I'm told. Since above 40 (ish) MPH isn't super usable for me (water too rough), I'll take the improved hole shot since my WOT is still in the 3800-4200 range spec'd by Mercruiser.