For those of you who have been following I had it fixed for a day. I'm beginning to think it is the output side of the lower unit.<br /><br />Here is what has been done,<br />First I fixed the lower unit water supply then several leaks that developed in the thermostat area thermostat was replaced. After two outings I discovered two cracks in the water chambers on the manifold no water in places where it is not suppose to be, so I thought I would try the cold weld stuff this work great BTW sealed it all up.<br />During this process I had taken every thing off to the block to make sure I got it all. Even took the water pump off to inspect it replaced the belt since it was on it's last legs cleaned out all the parts got a gasket kit (no water pump gasket)<br />Started it up on the muffs and now it runs to the 180/190 mark never did this before. Didnt go higher but before with the leaks it would run about 160 on muffs or in the water but on WOT it would climb to 240 on the water before I pull her back to cool off. So there is no point to take to the lake to see what happens at this time.<br /><br />When she is running now there are no more inboard leaks and there is lots of hot water coming from the area between the lower unit and intermediate unit where the two join but very little coming from the exhaust holes in the prop area.<br />All the flow rates are right according to the book. And it makes sense the guy who had her before said, if he lifted the lower unit with the tilt off the bottom it would cool fine, if there was a blockage in the exhaust side of the lower unit, as it would block the flow and when lifted it would flow fine as there seal between the lower unit and intermediate unit would be broken.<br />One thing though and Im going to get some heat test sticks to see what happens, but it just didnt seem to be that hot when I touched the motor. <br />Strange but true must be OMC.<br /><br />Any thoughts would be appreciated<br />Alex