Mothballed OMC 190 back on water - repair log

SeanMcl

Petty Officer 2nd Class
Joined
Apr 3, 2009
Messages
187
Just a post for posterity. Hope this helps someone else out.

The boat: 1974 Gulfstream, OMC 190 I/O. Has not been run in 6 years. Kept in indoor storage.

The pregame warm up: Pulled the spark plugs, put some oil in there, turned motor over by hand to make sure it's moving OK. Pulled the distributor, spun the oil pump with a drill for a minute or so. Gas tank was full of 6 year old gas, put two bottles of octane boost and a bottle of Sea Foam in it, changed the fuel filter, crossed my fingers. Put in a new battery. Checked oil levels in intermediate, upper and lower gear cases, had milky oil in the upper, drained and refilled upper case. Tuned on blower and bilge pump, both run.

Initial issues: Engine will not start.
Fuel leaking from carburetors accelerator pump gasket. Carb is a Holley 2bbl, list number is 6317-1. I can find almost no info on this carb on the net. I order Holley rebuild kit 703-30, which turns out to be wrong, 3-888 is the correct one, but I don't know that yet. :)
The distributor is in bad shape, a Prestolite IBM 7007S-11G. The local marine shop has a new cap, rotor, points and condenser for it though.
Now the engine starts, and seems to run fine. Take a quick trip to the nearest lake.

Secondary Issues: It doesn't want to start on the lake. After a couple shots of starter fluid, it fires up and runs OK. There is a major hesitation when the throttle is punched, but other than that it's good. After about 3 hours the engine kills while cruising at about 1/2 throttle. Restarts fine, then kills every 2 minutes or less on the way back to dock. Putting in a spare fuel filter did not help.

Came home, drained old fuel. Filled up with 91 octane and a bottle of carb cleaner. Next trip to the lake I have the same issues. It will run for up to 1/2 hour OK, then back to stalling every 2 minutes.

Thinking I still have carb trouble, I call Holley tech support and find I have the wrong renew kit in it. My carb is a 300 CFM 2 bbl specifically for the marine Ford 302. Put in the correct renew kit (3-888), also find clogged accelerator pump nozzles that I missed the first rebuild. Run back to the lake, and now it is running really well... for about 2 hours.

Third Set of Issues: The stalling is back, same as before. No acceleration bog though, which is good. I unscrew the fuel level plug in the float bowl, and it's dry in there. Must be the fuel pump, I think. No fuel in the pump's sight bowl, though, which I would expect if the pump had failed. Puzzled.

Come back home, buy a new fuel pump ($165? Yikes!), start searching the iBoats forums for fuel pump issues, and find an excellent article on troubleshooting fuel delivery issues with a a vacuum/pressure gauge.
I build a setup like is pictured in the article, place it between the fuel pump and the carb, and it slowly builds pressure to 3.5 lbs. Too low, looks like a bad fuel pump, I think. Then I put the gauge between the fuel pump and the gas tank to measure vacuum and it pulls over 21 inches of Hg! Wow, that's a bit high. I remove the pickup tube in the gas tank, and the screen is clogged so bad I can barely blow through it. When I try cleaning the screen it disintegrates, so I cut off what is left. I soldered some brass screen from a hose fitting back on the tube. I also put an additional fuel filter inline between the tank and the fuel pump because now I'm paranoid about gunk in my tank. I also replace all the fuel line from the tank to the carb. It was only about 6 feet, so not a big deal.

So I hook everything back up, and even with the additional fuel filter the vacuum gauge is pulling 2 inches of Hg. Fuel pressure is reading 5 psi. Fuel float level on the carb is proper. A quick trip out to the lake and all is running fine. Throttle response is improved as well. Knock on wood, I am calling the stalling and acceleration bog fixed.

4th Issue: Water in the upper gearcase oil. I took the boat to a mechanic for a new upper gearcase seal kit. Turns out that it's possible for water to get trapped in the impeller even with the outdrive down. The trapped water froze blowing out a couple seals in the impeller housing and buckling the plate the water pump impeller sits on. He replaced the impeller and plate, and put in the seal kit. Pressure tested it and everything held. He told me to unplug the ignition coil and then to spin the motor once with the outdrive down before storage and that would clear any trapped water out of the impeller housing preventing this kind of thing in the future.

I also found out that a bilge pump can run, but still not be able to pump any water. I replaced that too.
 

WizeOne

Commander
Joined
Mar 23, 2008
Messages
2,097
Re: Mothballed OMC 190 back on water - repair log

Good luck Sean. If you didn't already know it, the GulfStream is a great boat. Those things were made right in your backyard. Shame they didn't make it past some time in the eighties. Don't let any water get into your gas tank bay via the cutout at the forward bilge bulkhead. Also, do not run that OMC with the outdrive in any up position.

Other than that, you can stick your tongue out at all the black anchors when you are running tight circles around them or changing the prop (with boat in water) just sitting on your transom.

If that electric shift ever takes a crap, pick up the later '81-'85 mechanical shift drive and shift converter.
 

supercab78

Petty Officer 2nd Class
Joined
Sep 6, 2004
Messages
158
Re: Mothballed OMC 190 back on water - repair log

On my 1975 OMC I always poured a little antifreeze down the hose that leads to the impeller, and into manifolds and block just for cheap insurance. Do you still need a marine distributor?
 

WizeOne

Commander
Joined
Mar 23, 2008
Messages
2,097
Re: Mothballed OMC 190 back on water - repair log

All you Gulfstream guys should visit the 'Owners Groups By Manufacturer' section at the bottom of the main index page.

There is a Gulfstream Forum that is begging your input to. Start your own thread and put in some descriptions and pictures of your boats. There is no other place on the net where this is happening for the Gulfstream Brand.
 

SeanMcl

Petty Officer 2nd Class
Joined
Apr 3, 2009
Messages
187
Re: Mothballed OMC 190 back on water - repair log

WizeOne, I did know the Gulfstream was made in Salt Lake City. I've heard it's a well made boat, and this particular one has been in the family since 1982 or so. It's had 1 or 2 tilt motor failures in the 80's and 90's, the electric shift switch went out in the early 90's and we blew a driveshaft due to bearing failure (water in the upper gearcase) in about '98, but with the exception of the driveshaft incident it's always gotten us back to the dock under it's own power. I'm well aware of the damage to the ball gears that running them up does, we've always just coasted into the beach and paddled out if the water is shallow. They are so noisey when tilted up I can't believe anyone does it on purpose. When the upper case was changed in '98 the ball gears were replaced, and it's got less than 50 hours on it since then.

supercab78, I like the antifreeze idea. I don't think I need a new marine distributor, the tune up parts seem to have this one working fine. I have decided that if I ever need to replace it I'm switching over to something like Mallory's HEI marine unit. Until then I'm fine to run what I brung.
 

WizeOne

Commander
Joined
Mar 23, 2008
Messages
2,097
Re: Mothballed OMC 190 back on water - repair log

..... It's had 1 or 2 tilt motor failures in the 80's and 90's......

There is a way to keep that from happening. I'm still running the original tilt motor from 1975.
 

SeanMcl

Petty Officer 2nd Class
Joined
Apr 3, 2009
Messages
187
Re: Mothballed OMC 190 back on water - repair log

There is a way to keep that from happening. I'm still running the original tilt motor from 1975.

Point a brother to a link?
 

bruceb58

Supreme Mariner
Joined
Mar 5, 2006
Messages
30,537
Re: Mothballed OMC 190 back on water - repair log

One thing I would not have done was start out with 6 year old fuel. It would have been best to drain the tank and start fresh.
 

SeanMcl

Petty Officer 2nd Class
Joined
Apr 3, 2009
Messages
187
Re: Mothballed OMC 190 back on water - repair log

One thing I would not have done was start out with 6 year old fuel. It would have been best to drain the tank and start fresh.
It was a calculated risk. I calculated the hassle of doing it vs. opening a couple cans of chemicals. :)

In the end I ran the old fuel through my car and it was just fine, and if I had found the plugged up fuel pickup sooner I would have left the old fuel in the boat and probably not had any issues there either. Either way, it worked out OK.

BTW, if you ever get the chance to taste 6 year old fuel; pass. As bad a normal gas is, the old stuff is WAY worse. I am definitely buying one of those bulb things to get the flow started next time.
 

bruceb58

Supreme Mariner
Joined
Mar 5, 2006
Messages
30,537
Re: Mothballed OMC 190 back on water - repair log

Been in the same situation. I realize it was a hassle but I was so glad I did it. Unfortuantely, no chemiclas you can buy are going to restore the old fuel.
 
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