Bootkie2
Seaman Apprentice
- Joined
- Jul 16, 2018
- Messages
- 32
This season after logging 4 trouble free hours, I've now been chasing power/RPM/hesitation issues on my 06’ 496 Mag HO with 920 hours.
So far, I've done the following:
-scanned computer using Rinda for active fault codes / freeze frame data. There are No active codes or occurrences.
-Tested fuel pressure on the rail, getting 40-41psi even when it the engine bogs down.
-Removed/Inspected plugs, all looked pretty normal (not drenched in gas/oil)
-Replaced all spark plugs (since they were already removed, why not)
-Replaced IAC and IAC muffler
-Fuel and oil filters replaced right before spring launch on 5/15
-Ran engine connected to a clean external 6 gal fuel tank with fresh gas.
-Alternator testing FAILED, voltage all over the map, so threw in a new alternator and at least fixed that issue.
Still after all this work the hesitation is still there. I'll be cruising at 3000 RPM and then suddenly bogs down and hunts for RPM, (almost feels like when doing a cylinder drop test on the scan tool) so I slow down to headway speed and the engine sounds really really rough. Then it will recover for a few minutes, I'll add some more power then ,it bogs down again and sounds really rough. Repeat.......
I have not tested or done anything with the injectors. but it feels like that should be the next move. What do you all think think?
I'm trying not to think bad compression just yet but probably going to have to test it at some point.
So far, I've done the following:
-scanned computer using Rinda for active fault codes / freeze frame data. There are No active codes or occurrences.
-Tested fuel pressure on the rail, getting 40-41psi even when it the engine bogs down.
-Removed/Inspected plugs, all looked pretty normal (not drenched in gas/oil)
-Replaced all spark plugs (since they were already removed, why not)
-Replaced IAC and IAC muffler
-Fuel and oil filters replaced right before spring launch on 5/15
-Ran engine connected to a clean external 6 gal fuel tank with fresh gas.
-Alternator testing FAILED, voltage all over the map, so threw in a new alternator and at least fixed that issue.
Still after all this work the hesitation is still there. I'll be cruising at 3000 RPM and then suddenly bogs down and hunts for RPM, (almost feels like when doing a cylinder drop test on the scan tool) so I slow down to headway speed and the engine sounds really really rough. Then it will recover for a few minutes, I'll add some more power then ,it bogs down again and sounds really rough. Repeat.......
I have not tested or done anything with the injectors. but it feels like that should be the next move. What do you all think think?
I'm trying not to think bad compression just yet but probably going to have to test it at some point.