flyingglasses
Cadet
- Joined
- Jun 12, 2023
- Messages
- 10
Hi all,
I’ve been working on a 1995 evinrude E15 and had some troubles last fall with the idle. Over the winter I disassembled and cleaned the carb and installed the extended idle plugs as the QL77JC were fouling after a few hours as I troll extensively. I took the boat out the other day and set the idle unrestrained in the water and in gear it was running at about 900 RPM very nicely. After about 2 hours the idle was bogging down into the mid 600s and stalling. It would restart no problem but then slowly bog down and stall around 650 RPMs. I almost decided I was done for the day at that point and wanted to go home and back to the drawing board. Instead I decided I wanted to go try one fishing spot up the river before I cut my day short so I went full throttle up the river for about 10 minutes, no issues. When I got to my spot and brought the throttle back to idle it wouldn’t go below about 1500 RPM and was close to 2000 RPM in neutral. I made no adjustments, just went WOT for a few minutes. Anyone have any ideas or suggestions on what I have done to this motor?
Thanks
I’ve been working on a 1995 evinrude E15 and had some troubles last fall with the idle. Over the winter I disassembled and cleaned the carb and installed the extended idle plugs as the QL77JC were fouling after a few hours as I troll extensively. I took the boat out the other day and set the idle unrestrained in the water and in gear it was running at about 900 RPM very nicely. After about 2 hours the idle was bogging down into the mid 600s and stalling. It would restart no problem but then slowly bog down and stall around 650 RPMs. I almost decided I was done for the day at that point and wanted to go home and back to the drawing board. Instead I decided I wanted to go try one fishing spot up the river before I cut my day short so I went full throttle up the river for about 10 minutes, no issues. When I got to my spot and brought the throttle back to idle it wouldn’t go below about 1500 RPM and was close to 2000 RPM in neutral. I made no adjustments, just went WOT for a few minutes. Anyone have any ideas or suggestions on what I have done to this motor?
Thanks