2000 Johnson 200 Ocean Pro - Out Of Ideas... Please Help

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
Facts at a Glance

Symptoms
  • Rough Inconsistent Idle
  • Requires High Idle Setting to Run in Water
  • Can Rev on Hose But Stalls on Throttle Up in Water
  • Low Compression
  • Miss on Cylinder 4
Parts Replaced - All OEM
  • New CDI
  • New Stator
  • Used Fly Wheel
  • Full Carb Rebuild Kits
  • Full Water Pump Rebuild
  • Fuel Pump Piston Rebuild Kit
  • New Fuel Lines and Clamps
Tests and Inspection
  • Spark
  • Compression - Methodology
  • Reed Valves
  • Intake Manifold
  • Fuel Rail
  • Fuel Lines
  • Tested with External Fuel Tank
  • Carb Mating Surfaces
  • Timer Base
Tuning
  • Link & Sync
  • Idle Timing
  • Throttle & Shift Linkage
  • Floats
Known Issues
  • Low Compression - 68-78
  • Miss - Cylinder 4?
  • Lower Unit Wobble
    • Scoring on Drive Shaft
    • Water Pump Housing Deformed
    • Seals Stretched and Deformed
    • Exhaust Gaskets Need Replaced
 

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
Full Narrative

I’m trying to help out a friend with his outboard. Nearly every part has been replaced or rebuilt except the motor itself. But it still wont run right. It’s been to every local outboard shop and mobile mechanic that will work on it. Nobody’s been able to figure it out. We’re at our wits end and need the help of the iBOATS community.

CDI
Before I started working on it it had the CDI replaced. The lower unit was also replaced with a an SEI remanufacture. The wiring of the CDI looks correct. I’ll touch on what I found with the lower unit shortly; I’d like to go in the order I troubleshooted.

Flywheel
The owner advised that a previous mechanic had, “epoxied the magnets on the fly wheel”; The motor would turn over and fire up but there were obvious problems with timing and it would quickly come to a clunking halt.

The owner didn’t have a lot of details about the magnets. He wasn’t sure if they’d come loose, completely off or why they needed to be epoxied.

I found the magnets had in fact been reattached, but the placement was off. So we bought a replacement.

Stator
The stator was in bad shape. Much of the resin had melted off and there were signs of some sort of impact. I only did a visual inspection. I did not test it. He already planned on replacing it for good measure and it was on its way.

I cleaned up the melted resin and inspected the timer base. It moves smoothly and freely without any signs and hesitation. I installed the new stator and flywheel. It fired up after that and the timing problems subsided. But it was still running very rough. I was able to keep it running long enough to set the idle timing. There were timing marks on TDC and 4 degree ATDC (factory spec idle). But the WOT mark at 18 degrees BTDC was missing. I manually confirmed the TDC mark was accurate and then set idle timing to spec.

Water Pump
After achieving an idle consistent idle, I noticed there was no stream from the tell-tail. There was little to no water coming out of the exhaust as well so we ordered a full water pump rebuild kit.

I noticed that the top seal was all stretched out. I also noticed a gap between the shaft and the top opening of the housing, maybe about a millimeter in size. The impeller was shredded. I fished out the loose chunks of rubber and flushed it out using the flush port. I haven’t pulled the water jacket or heads so I don’t know if I got everything.

As I pulled what remained of the impeller off of the driveshaft, it got stuck. I discovered the drive shaft was scored where it had come in contact with the water pump housing. And the bottom opening had been ground from a circle to an egg shape and a bur had formed. The wobbly shaft must have caused, or at least contributed, to the scoring I found. I did my best to sand it smooth and rebuilt the pump.

I advised the owner of the problem. He called SEI and they told him, “It’s good for a drive shaft to be wobbly”. I’m not the most seasoned marine mechanic, but I have rebuilt dozens of water pumps and never seen a drive shaft with that much play.

Link & Sync
With the motor being properly cooled from the pickup, I was able to do a link and sync and achieve a decent idle. But it would randomly stall. I noticed a miss when it was running and the miss seemed to cause, or contribute, to the stall. I started pulling spark plug wires until I isolated the miss to cylinder #4. With that plug wire pulled the motor seemed to smooth out and. The miss went away and it stalled less. I could even rev it a little but it was still running rough and occasionally stalled.

Carburetor Rebuild
Setting the miss on cylinder 4 aside, it felt like there was a fuel delivery issue. I pulled one carb and discovered a few problems; the gaskets were intact with no holes, tears or fatigue cracks, but some were partially collapsed where the channels are. I also found a lot of oil (in retrospect this should have led me straight to the VRO).

I’ve seen carbs in worse shape running better but I recommended we rebuild the carbs. We used all OEM kits with new floats, pins and seats. I was careful to set the floats parallel to the housing. I also visually inspected the bowl and manifold mating surfaces because I know these plastic OMC carbs are prone to warping. They looked fine so I reassembled them.

I inspected the fuel rail for leaks and then rebuilt it with brand new fuel lines and spring clamps. I also replaced all of the zip ties with spring clamps on every fuel line between the tank and the fuel pump with the exception of the main line which has screwed clamps.

Before reinstalling the carbs, rail and lines, I visually inspected the reed valves. They looked brand new. The intake manifold gasket looked brand new as well. I’ll bet they were both replaced as someone was chasing the problem I am.

With the carbs reinstalled, I was able to get a hard primer bulb. The motor fired right up and idled well enough to do another link & sync and reset the idle timing. I felt like it was ready for a water test & tune.

1st Water Test
Immediately before driving to the boat ramp, I started and idled the motor on muffs for 15 minutes. It only stalled once shortly after it started as it settled down to a lower idle. It was still smoking a lot more than it should but it was running well enough for a water test/tune.

In the water the motor that had started on the 1st key turn and idled well would barely even start. It would turn over and fire but then immediately stall. The only way I was able to keep it running was to bring the idle way up. After running for a while I was able to reduce the idle down low enough to safely shift into gear. So I took her out to see if I could throttle up.

She idled beautifully all the way through the no wake zone. But the moment I tried to throttle up she hesitated, sometimes backfired and stalled. It was also smoking really bad. I had the air fuel mixture set to 7 full tuns (the middle between factory spec 6-8). I adjusted up and down but could not find a setting that the motor liked better. I’ve since found she likes 6 ½ turns best.

Compression Check
Back on dry land, I wanted to make sure we’re working with a viable motor before proceeding. I know, this should have been done sooner. The results were not encouraging at 68-78 (only one was at 78). Based on the miss I’d seen I thought I might find lower compression on cylinder 4, but it was in line with the rest at 72. I can post pics of the results.

I’ve seen compression improve with use so, after advising the owner it may be due for a rebuild, I continued trying to get it running in the hopes that it would improve once we could get it to run at WOT and clean itself out.

Fuel Pump
Still convinced that I’m dealing with a fuel delivery issue, the next logical step was to inspect the VRO (I’ll bet most of you reading this arrived at that quicker than I did). Live and learn. And the carbs did show signs of needing a rebuild anyway.

I started by pulling just the oil pump, it looked fine. So I pulled the front off of the fuel pump and had an ah-ha moment. The rubber around the piston had two fatigue cracks, one about two 3 centimeters long. This has to be the source of the fuel delivery issue, excessive smoke and oil I found in the carbs and oil rich / gas lean state I was seeing.

We couldn’t find a full rebuild kit that included the diaphragm so we ordered the only thing we could find… a piston rebuild kit. I was so sure I’d finally found the problem I didn’t even bother pulling the pump and inspecting the diaphragm. I rebuilt the piston replacing the seal and o-rings and reassembled the VRO. I was able to achieve a rock hard primer bulb. You can literally stand on the damn thing. And it stays hard with the motor running… like a teenager on Cialis.

2nd Water Test
There was no doubt in my mind that we’d found and fixed the fuel delivery issue. I was 100% convinced that the motor could be water tuned and the WOT timing set. So I invited the owner out on the water to help. I was so excited to see his reaction when it ran well for him for the very first time since he’s owned it. And flabbergasted when it did the exact same thing as it had on the first water test. I couldn’t even get it to start and stay running without cranking the idle way up. I found an idle that minimized stalling and still allowed us to shift, so we pulled away from the dock. It barely made it out of the no wake zone before stalling. Then I couldn’t even get it to idle again, much less throttle up.

I don’t know what to try next. Do I back track to double check my work? I pulled two of the carbs to adjust the floats and they looked perfect. I haven’t pulled the fuel pump back apart because I know it’s pumping well.

I apologize for the long post. I tried to list everything without being verbose. I failed miserably. If you made it this far, I thank you very much. I appreciate any help you’re inclined to offer.
 

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
Had to create two posts because the 10000 character limit error; even though the the whole post (both parts together) are only 9616.
 

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
That's a fair criticism.

It probably seems like we're just throwing parts at the problem. But that's not the case. When troubleshooting an unknown issue, I always start with the basic three; spark, compression and fuel. But initially, this was not an unknown problem.

I was told from the start that the magnets on the fly wheel had been epoxied. So of course that's the first thing I'm going to examine. When I pulled the flywheel and found damage to it and the stator (obvious impact marks on both) why would I keep cranking it and risk more damage to do a compression check?

I agree that a compression check should have been done sooner and mention that in my initial post. It probably should have been done after the flywheel was replaced. Maybe we got a little too excited to hear it run for the first time. And, until things progressed, there was no indication it may have low compression.

Once it was running it became obvious that the water pump was not working. While I could have just used the flush port to continue troubleshooting it on a hose, I knew we would eventually be testing it in the water so why not replace the water pump? It's a cheap easy repair.

I know my post was crazy long. And I don't expect anyone to read every word. But I did mention that this owner has a sentimental attachment to the motor and wants it running at all costs including a full rebuild if necessary.

I cautioned the owner every step of the way, before every part order and before we even knew it had low compression. He'd already put more into the motor than it was worth, was aware of that, and committed to continue until it was fixed.
 

havoc_squad

Senior Chief Petty Officer
Joined
Mar 5, 2011
Messages
738
That's a fair criticism.

It probably seems like we're just throwing parts at the problem. But that's not the case. When troubleshooting an unknown issue, I always start with the basic three; spark, compression and fuel. But initially, this was not an unknown problem.

I was told from the start that the magnets on the fly wheel had been epoxied. So of course that's the first thing I'm going to examine. When I pulled the flywheel and found damage to it and the stator (obvious impact marks on both) why would I keep cranking it and risk more damage to do a compression check?

I agree that a compression check should have been done sooner and mention that in my initial post. It probably should have been done after the flywheel was replaced. Maybe we got a little too excited to hear it run for the first time. And, until things progressed, there was no indication it may have low compression.

Once it was running it became obvious that the water pump was not working. While I could have just used the flush port to continue troubleshooting it on a hose, I knew we would eventually be testing it in the water so why not replace the water pump? It's a cheap easy repair.

I know my post was crazy long. And I don't expect anyone to read every word. But I did mention that this owner has a sentimental attachment to the motor and wants it running at all costs including a full rebuild if necessary.

I cautioned the owner every step of the way, before every part order and before we even knew it had low compression. He'd already put more into the motor than it was worth, was aware of that, and committed to continue until it was fixed.
This is why more service centers will decline to do such work no matter how much money customer gives to load the parts cannon.

That is because very likely, they will turn on you at the end when that fails to work and blame you for the issue.

It is a bad business model that hurts a shop's reputation and ability to pay the bills.

Many service shops make it their policy that if low compression and fails leak down test and is confirmed to not be a head gasket failure, full rebuild or they stop work on it.

Many will only rebuild outboards or inboards where warranty coverage covers their labor as well.
 

dingbat

Supreme Mariner
Joined
Nov 20, 2001
Messages
16,083
I would not put another dime into that motor until you get the compression sorted out. It's never going to idle with compression numbers like that.

Twenty years and two power heads and counting on Evinrude Ocean.
It's been a decent motor but its been problematic at times. Fortunately my mechanic is/was a factory Evinrude guy with twins of the same motor on his boat.

Intermittent high speed miss
New flywheel - Intermittent miss. problem never found

Wouldn't idle at spec rpm in the water
New carb stack and manifold - hair line cracks found in 4 carbs

Although spec is lower, neither power head like to idle below 750 RPM
 

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
I would not put another dime into that motor until you get the compression sorted out. It's never going to idle with compression numbers like that.

Thank you for your reply.

It idles fine right now with compression that low.... on the hose. In the water not so much. But if you crank up the idle screw it will idle in the water too. I have video of both. The short term problem we're try to solve is bogging and stalling when throttling up on the water. And of course the fact that it won't idle at the same setting on water as on the hose.

We'll likely end up rebuilding it. In the mean time, do you really think the symptoms I've described are entirely due to low compression? I've seen motors run with similar compression. Heck, I own a 2-stroke Yamaha with 70ish across all cylinders that fires up cold on first key turn and runs fine after sitting for months. It's never given me a single problem and I've done nothing to it.

I really feel like it's something else. I should still be able to make some power with 70psi. At lease there isn't a huge variance. I haven't checked compression since the carb and fuel pump rebuilds. Maybe it went up? I've read post where that's happened. I'll check it again and report back.

I mean, I haven't checked everything yet. Like coils. Plugs and wires look brand new so I haven't considered them. I know it's hard to know what to check next after so much has been done. I was just hoping to get some guidance or suggestions from someone with more knowledge and experience than me. I'm not a professional mechanic. I'm just trying to help out a friend. And I enjoy getting old boats back on the water.

BTW: I have pictures and video of everything. I just haven't posted them because I've done such a huge information dump already I didn't want to overwhelm readers further with a crap ton of videos to watch too. But I'm happy to post video of it running on the hose and on the lake, videos of the rebuilds, pictures of every part, or anything else that might help you help me.

Thanks again.
 
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havoc_squad

Senior Chief Petty Officer
Joined
Mar 5, 2011
Messages
738
Thank you for your reply.

It idles fine right now with compression that low.... on the hose. In the water not so much. But if you crank up the idle screw it will idle in the water too. I have video of both. The short term problem we're try to solve is bogging and stalling when throttling up on the water. And of course the fact that it won't idle at the same setting on water as on the hose.

We'll likely end up rebuilding it. In the mean time, do you really think the symptoms I've described are entirely due to low compression? I've seen motors run with similar compression. Heck, I own a 2-stroke Yamaha with 70ish across all cylinders that fires up cold on first key turn and runs fine after sitting for months. It's never given me a single problem and I've done nothing to it.

I really feel like it's something else. I should still be able to make some power with 70psi. At lease there isn't a huge variance. I haven't checked compression since the carb and fuel pump rebuilds. Maybe it went up? I've read post where that's happened. I'll check it again and report back.

I mean, I haven't checked everything yet. Like coils. Plugs and wires look brand new so I haven't considered them. I know it's hard to know what to check next after so much has been done. I was just hoping to get some guidance or suggestions from someone with more knowledge and experience than me. I'm not a professional mechanic. I'm just trying to help out a friend. And I enjoy getting old boats back on the water.

BTW: I have pictures and video of everything. I just haven't posted them because I've done such a huge information dump already I didn't want to overwhelm readers further with a crap ton of videos to watch too. But I'm happy to post video of it running on the hose and on the lake, videos of the rebuilds, pictures of every part, or anything else that might help you help me.

Thanks again.
This is why you do a leak down test at TDC for each cylinder.

This tells what compression tester will not say without resorting to cylinder and piston inspection.

Anything more than 20% leakage in any cylinder is becoming a mechanical running issue. Over 30%, unless it is a gasket or head failure, that is definitely rebuild or replace power head territory.

You want a more clear picture of cylinder health, do a leak down test.
 
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flyingscott

Fleet Admiral
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Apr 8, 2014
Messages
8,095
good luck with your motor since you don't want to deal with the compression issue I cant help you
 

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
good luck with your motor since you don't want to deal with the compression issue I cant help you
That's okay flyingscott. You weren't trying to help. Thanks anyway.
This is why you do a leak down test at TDC for each cylinder.

This tells what compression tester will not say without resorting to cylinder and piston inspection.

Anything more than 20% leakage in any cylinder is becoming a mechanical running issue. Over 30%, unless it is a gasket or head failure, that is definitely rebuild or replace power head territory.

You want a more clear picture of cylinder health, do a leak down test.

Thank you havoc_squad! I really appreciate your suggestion. I'll take your advise and post my findings.
 

flyingscott

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Messages
8,095
That's okay flyingscott. You weren't trying to help. Thanks anyway.


Thank you havoc_squad! I really appreciate your suggestion. I'll take your advise and post my findings.
A leak down test isn't going to tell you anything your compression test has not told you already. Hopefully you are not charging for your time. Might be time to sack up and take the head off instead of looking for a Unicorn cure. Or try being honest with the guy about his boat anchor
 

racerone

Supreme Mariner
Joined
Dec 28, 2013
Messages
37,846
You are doing all this work ?----It is so simple and cheap to pull cylinder heads to inspect for scored cylinders.
 

dingbat

Supreme Mariner
Joined
Nov 20, 2001
Messages
16,083
It idles fine right now with compression that low.... on the hose. In the water not so much.
To me, that falls under the category of doesn't idle.

What RPM are you idling at on the hose?
Mine idles 1,250 -1,300 rpm on hose, 725-750 rpm in the water
I really feel like it's something else. I should still be able to make some power with 70psi. At lease there isn't a huge variance.
All cylinders on mine are between 98 and 105 psi.
Either your gauge is out of calibration or down 30% in compression.
 

flyingscott

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Apr 8, 2014
Messages
8,095
Cmon people, Did anybody even read what was wrong with this motor?
The water pump housing was deformed.
the exhaust gaskets leak.
This motor sounds to be seriously overheated and damaged.
There is probably at least $1500 in parts and it runs no better. This motor has had the parts cannon loaded and the OP refuses to address the compression issue. This whole thing sounds Sketchy.
 

Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
48
To me, that falls under the category of doesn't idle.
Except that it does idle. Not perfectly but it idles.

This is how it ran on the hose just before the 2nd water test.


What RPM are you idling at on the hose?
Mine idles 1,250 -1,300 rpm on hose, 725-750 rpm in the water

Mine is almost the polar opposite. About 800 rpm on the hose. But I have to adjust it al the way up to 1200 on the water to keep it from stalling until it warms up. Then I seem to be able to lower it down to 800.

The 1st water test.

 
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Blowinup

Seaman Apprentice
Joined
Sep 1, 2021
Messages
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To me, that falls under the category of doesn't idle.

What RPM are you idling at on the hose?
Mine idles 1,250 -1,300 rpm on hose, 725-750 rpm in the water

All cylinders on mine are between 98 and 105 psi.
Either your gauge is out of calibration or down 30% in compression.

Yes, we know the compression is low. From what I can gather a 2-stroke of this age should be between 90-120. We know this. My point isn't that it's fine and dandy at 70. My point is that a motor with 70 can still produce power if everything else is working well. Which is why I want to address anything else that might be wrong and maybe get a little life out of it until the motor can be rebuilt or replaced.

I also don't want there to be a single issue to deal with after a rebuild. The owner has really been through the ringer with this motor. It would suck if he paid for a rebuild and still had issues.

It is possible BTW that my gauge is off. It's from Harbor Freight.
 
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racerone

Supreme Mariner
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Dec 28, 2013
Messages
37,846
Take heads off and have a look at cylinders , or too much trouble to do that ???
 

tphoyt

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Jun 10, 2010
Messages
1,270
There is nothing to be intimidated by here.
If you have done all the other work you will have no problem with pulling the heads for inspection.
I have been following along with a lot of wondering why all this is being done with these low numbers and the overwhelming possibility of a serious overheat. Your harbor freight gauge could very well be off. If you can’t invest in a quality gauge most auto parts stores will loan them out with a deposit. It’s very important to get an accurate number here. If they are truly that low my personal opinion giving there is sentimental value in this motor would be a rebuild, find a donor motor with known good compression or get a short block and swap over all the new parts. As I’m sure you and the owner know you rarely get a return on your investment when doing things for sentimental reasons.
Best of luck to you both.
 
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