Compression last checked in March 2021 was 90psi Upper Cylinder, 95 Lower Cylinder. Was running OK but had a Slow Speed Cough which I eliminated in September by backing out the Slow Speed Screw by 1 1/2 turns (seemed like a lot at the time but made engine run better in water tank). In November engine ran poorly--Upper spark plug seemed fine, lower plug appeared fouled. I replaced both plugs using L77JC4 (best guess these plugs were at least 3-4 years old although probably had less than 1 hours on them). Past week ran engine again, it still runs poorly. Seems to have a lot of unburnt fuel dripping out of exhaust after 30-40 minutes runtime on new plugs. Top plug is definitely fouled, lower plug looks nice Tan color. Using adjustable Spark tester each Cylinder is getting blue spark greater than 3/8 inch. Both pistons are moving ( I haven't borrowed a Compression Gage yet) i.e. no Broken Rod, etc.
Another engine runs fine using this same Fuel Tank, Bulb and Fuel Line. Pumping the bulb while engine was running rough did not make any difference.
So what should I look for as I further investigate? I have never cleaned/rebuilt the Carb on this motor (which I acquired about 5 years ago). I am thinking that is needed or (as a minimum) turn the Slow Speed Screw back in at least 1/2 turn, then on-the-water test.
Another engine runs fine using this same Fuel Tank, Bulb and Fuel Line. Pumping the bulb while engine was running rough did not make any difference.
So what should I look for as I further investigate? I have never cleaned/rebuilt the Carb on this motor (which I acquired about 5 years ago). I am thinking that is needed or (as a minimum) turn the Slow Speed Screw back in at least 1/2 turn, then on-the-water test.