Boat is a 1984 17' Sunrunner with a 1984 mercruiser 140 inline 4cyl 3.0L engine.
Single adjusting screw mercarb 2bbl
I purchased The boat about 3 months ago, the first couple times I took it out it ran great, cold started good, didn't miss fire, idled smooth, restarted warm good.
I noticed one day gas was very minor seeping out of the float gasket between the 2 carburator half's. I purchased a rebuilt carburator, then swapped it out with another rebuilt carburator and can't get it to run right at idle or starting.
The engine seems to be running rich at idle, you can smell gas and iv tried different plugs and they are always all black. it will not start at all just caughts cold (when the choke is on). If you turn the key on to let the choke preheat and open it will start once choke is fully opened but still is missing at idle and smelling rich exhaust. Once off of idle it runs smoothly through out the throttle range. It will restart good warm if choke is fully off but still be missing and stumbling.
Idle mixture adjustment that's supposed to be at 1 1/4 out has almost zero effect on running condition except if you screw it past 2.5 turns out it will really flood and die. You can screw it all the way in lean and it has little to no effect. it will still be running and missing.
Cap and rotor look Good- somewhat new
Plug wires look recently replaced
Plugs are new oem
Distributor has petronix electronic ignition
Compression is 132-133-132-132
Spark timing has little effect on missing at idle/ rich idle. I've tried 6° through 14° advance. Spec is 8° seems to do best at 12° advance.
yesterday I installed the spring loaded needle and seat it didn't help
I've played with float adjustments and adjusted then with a micrometer and they were already right on spec
Can you help me find what I'm missing?
Single adjusting screw mercarb 2bbl
I purchased The boat about 3 months ago, the first couple times I took it out it ran great, cold started good, didn't miss fire, idled smooth, restarted warm good.
I noticed one day gas was very minor seeping out of the float gasket between the 2 carburator half's. I purchased a rebuilt carburator, then swapped it out with another rebuilt carburator and can't get it to run right at idle or starting.
The engine seems to be running rich at idle, you can smell gas and iv tried different plugs and they are always all black. it will not start at all just caughts cold (when the choke is on). If you turn the key on to let the choke preheat and open it will start once choke is fully opened but still is missing at idle and smelling rich exhaust. Once off of idle it runs smoothly through out the throttle range. It will restart good warm if choke is fully off but still be missing and stumbling.
Idle mixture adjustment that's supposed to be at 1 1/4 out has almost zero effect on running condition except if you screw it past 2.5 turns out it will really flood and die. You can screw it all the way in lean and it has little to no effect. it will still be running and missing.
Cap and rotor look Good- somewhat new
Plug wires look recently replaced
Plugs are new oem
Distributor has petronix electronic ignition
Compression is 132-133-132-132
Spark timing has little effect on missing at idle/ rich idle. I've tried 6° through 14° advance. Spec is 8° seems to do best at 12° advance.
yesterday I installed the spring loaded needle and seat it didn't help
I've played with float adjustments and adjusted then with a micrometer and they were already right on spec
Can you help me find what I'm missing?