Well my face is red. Swapping the fuel lines did the trick. Unfortunately the "water jacket gasket" is still weeping around the plugs. The whole reason I did any work to the motor was to fix the leak. It's not too bad so I think I'm going to try some sealant to get it to stop. I did a compression test as well, these are my results... 95,100, 100, 105. I think I'm barely in spec between cylinders 1 and 4 (using a harbor freight gauge). Do those numbers tell me a whole lot? Hopefully in the next few weeks I can get it out on the water to do an actual test run.