Besegen
Seaman
- Joined
- Jan 28, 2013
- Messages
- 57
I've been following the forums for a few weeks now (since I bought my first real boat) but this is my first time posting.
I have deck boat with a 1975 85 Evinrude. A family friend completely restored it and he had it out only a few times since, but he insists this worked fine when he did.
I have had the boat out three times now and cannot get it to reverse. I changed the lower unit grease before the first trip and double checked (re-topped it off) after that just in case. It shifts to neutral and forward both just fine and the motor starts and runs like a charm other than not shifting to reverse. I have adjusted the linkage on the cable until it was maxed out and took us out of being able to shift to forward and it still would not go. I had seen some people talk about the grease being low so we checked that after the first go round and made sure it was topped off as I said. Immediately after that we adjusted the linkage until the prop locked in reverse, put the muffs on, fired it up and went to reverse. The prop instantly reversed its rotation. We gave it a little throttle for just a moment (didn't want to be throttling up with just the muffs) to make sure the prop rpms increased when we throttled and it did.
We were positive we had it whipped but got it back to the lake, dipped the boat in and fired it up and still...the boat would not reverse today.
I popped the hood again, took the shift bar off and shifted in by hand. It when in and shifted easily. I kept it there and readjusted the linkage to try to match it up and again I maxed out the adjust and was still falling maybe an 1/8" or less of being able to connect back to the bar. The forward and neutral though are both off again at this point too.
I'm at a loss about 1. What needs to be done to gain that 1/8" (less) bar but still get my forward and reverse back to right. and 2. Why it seemed to engage just fine with the muffs out of the water but when we dip it in it won't.
The previous owner says he never used it in cold weather. The water temp has been between 32 and 36 at most the three times were out and air temp between 40 and 50 degrees each time. He is hung up on thinking maybe the grease is too thick, or cold shrinkage of parts, or both is keeping it from engaging. Is this possible? I know the theory is there but I don't know that it would shrink that much (at least 1/4" from engaging in his linkage original position). I also think the motor and grease would warm up after buzzing around awhile and you would get it back later in the trip if that was the case. Trip 2 we did go ahead and go out for awhile and never did get it to engage later. But what do I know, I'm a greenhorn at this. Any help would be appreciated.
I have deck boat with a 1975 85 Evinrude. A family friend completely restored it and he had it out only a few times since, but he insists this worked fine when he did.
I have had the boat out three times now and cannot get it to reverse. I changed the lower unit grease before the first trip and double checked (re-topped it off) after that just in case. It shifts to neutral and forward both just fine and the motor starts and runs like a charm other than not shifting to reverse. I have adjusted the linkage on the cable until it was maxed out and took us out of being able to shift to forward and it still would not go. I had seen some people talk about the grease being low so we checked that after the first go round and made sure it was topped off as I said. Immediately after that we adjusted the linkage until the prop locked in reverse, put the muffs on, fired it up and went to reverse. The prop instantly reversed its rotation. We gave it a little throttle for just a moment (didn't want to be throttling up with just the muffs) to make sure the prop rpms increased when we throttled and it did.
We were positive we had it whipped but got it back to the lake, dipped the boat in and fired it up and still...the boat would not reverse today.
I popped the hood again, took the shift bar off and shifted in by hand. It when in and shifted easily. I kept it there and readjusted the linkage to try to match it up and again I maxed out the adjust and was still falling maybe an 1/8" or less of being able to connect back to the bar. The forward and neutral though are both off again at this point too.
I'm at a loss about 1. What needs to be done to gain that 1/8" (less) bar but still get my forward and reverse back to right. and 2. Why it seemed to engage just fine with the muffs out of the water but when we dip it in it won't.
The previous owner says he never used it in cold weather. The water temp has been between 32 and 36 at most the three times were out and air temp between 40 and 50 degrees each time. He is hung up on thinking maybe the grease is too thick, or cold shrinkage of parts, or both is keeping it from engaging. Is this possible? I know the theory is there but I don't know that it would shrink that much (at least 1/4" from engaging in his linkage original position). I also think the motor and grease would warm up after buzzing around awhile and you would get it back later in the trip if that was the case. Trip 2 we did go ahead and go out for awhile and never did get it to engage later. But what do I know, I'm a greenhorn at this. Any help would be appreciated.