Starboardlean
Seaman
- Joined
- Feb 15, 2016
- Messages
- 73
25553b... This was a no compression project. Blown head gasket fixed. Magneto plate wobbling. Fixed. Point gap problem fixed. Gummy Carb, fixed.Now she is easy starting..Today was her big sea trial. 10 miles up river and back. And she did fine, a little lacking in low to mid range. No bogging spitting etc. Just not quite the snap I expect. I ran her a few minutes with hood off to keep eyes on things, mainly magneto plate for wobble.All was good, maybe a better grease so timing will advance slicker, but a small victory. Put the hood on to quieten the ride. Yeah it was quieter. Felt slower to, I wrote that off to imagination. Nope, feels slower. Hood off, she is faster, no doubts. Inspected hood and inside is covered in 2 stroke juices.Slimy on block some to. In my 275 gal tank I went around seams with carb spray while she was idling, and got no hits. Reason being is I have low speed adjusted almost 3 turns out to stop a lean sneeze. I figured every motor is different, although that it a far cry from 1.5 turn. So I am running rich, got exhaust leak, which I assume is also by nature a vacuum leak, the source of my lean sneeze....correct??Back home tear her down to bare block. What do I find? Billy Bob prior owner JB welded bottom port side between crank case and block seam. No physical damage, just Jerry rigged. Sorry for the rant. 2 steps forward, 1 step back with this project. But forward progress overall.
Any leads on gasket between crankcase and block, the one I need??
Any leads on gasket between crankcase and block, the one I need??