Mikey N.C.
Seaman
- Joined
- Feb 14, 2020
- Messages
- 63
Ok. Update, ran motor today on muffs instead of direct hook up on motor side. Ran motor at 1800 rpm for about 30 mins. shut down , waited about 30 mins. pulled #4 spark plug , pulled kill switch, turned motor over no water coming out #4. It didn't make oil. Sucked out oil and changed filter. Fired motor back up on muffs, for 30 mins. at 2300 rpms. Oil was like new, a suprise to me, it's usually 4 oil and filter changes to clear. I'm guessing it was so full of mixed oil, that it cleared that quick. So steel gasket was reused at riser elbow (don't know if it's was a MLS gasket, don't look like one, just thin metal) I replaced with graphite type. I'm replacing seawater impeller at crank, had a o-ring leak. Will test in lake after.