With the first day of College Football yesterday, I got NOTHING done on the boat. But I made up for it today.
I got a bunch of trash cleaned out of the boat, got everything on the console disconnected. The in and out hoses on the livewell were a TOTAL pain! I ended up having to cut the in hose off. I hope it is still long enough when it is time to go back on... The console is WAY to heavy to get out of the boat by myself, so I'll have to wait on some help. Unfortunately, I still live in the city... ALL of my friends have moved to the 'burbs, and would rather lop off an arm than come into town... I dont blame them.
The major victory for today was the removal of the fuel tank. I had previously dug all of the foam from around the tank. Today I got all of the fuel (6-8 gallons) pumped out. Then I took a pice of metal and dug out from under the front corners. I looped a piece of rope under the front corners and tied ends together. I then stood where the console was and looped the rope loop over my hands and under my elbows. I then squatted ant levered the tank out. It was stuck pretty good at first but after about 10 secs of hard pressure, it popped right out.
The tank had been installed in an interesting way. It was between the stringers and closed at the front and rear by bulkheads. Then there was a now non-existent piece of plywood about 6 inches wide that was riveted to the ribs in the floor. Then two 1/8 inch thick by 1 inch wide rubber strips laid on the wood. Then they dropped in the tank and screwed wooden blocks to the bulkheads to hold the tank down. After that they poured in the foam down the inside edges of the stringers. This of course allowed the foam to run under the tank. as it expanded, it blocked all of the drainage holes under the ribs as well as all of the holes on the stringers that allowed water to drain down into the bottom of the hull. Even with "all" of the foam removed, this sucker holds water bad. Some drain clearing and redesign is in order. I read somewhere that 1986 was the first year of the pour in foam. The hull drains were obviously not designed with pour foam blockage in mind. You can see in the 3rd and 4th pics how the water is just standing in place. Gonna have to do something about that. The 5th pic shows the tank out. I took that pic after dark with the flash. So it really brought out the white "fuzz" corrosion. It is nowhere near as bad as it looks in the pics. There are 4 or 5 holes, but they are all about the size of a BB. I have a fantastic TIG guy that specializes in welding thin aluminum. He should be able to tank it and weld it up.