Hello all, need some help and advice. Got a 01 SeaRay 182 with 4.3 Mercrusier serial number M071272.
Bought the boat from a "boat club" (this was not a club boat, just something the owner picked up to "flip"). The engine has about 350 hours on it so Im guessing it sat around quite a bit all those years. We test drove it on the water and I checked out as much as I could on my own and I took her home about 3 weeks ago. We took the boat out the first weekend and it ran great but noticed that the starboard side riser was running really hot and the steering was really stiff which I knew already but tried to lube it up with no luck. While I did have it out, it ran great. Got up to plane just fine and temp stayed about 168 or so. I brought it back and he agreed to replace the steering cable and manifold. Before I bought it he already replaced the riser/elbow so that was already new.
Two weeks later I go to pick it up and he along with his "tech" was still working on it. This is where it got interesting for me.
While he did replace the steering cable and got a new manifold, he did not bother to order a new 3 inch riser which even to my untrained eyes looked like crap. Full of rust and the mating surface between the exhaust and water passages were not smooth at all. He was also using some orange Permatex stuff all over everything! The manifold gasket and between the spacer and riser/elbow were oozing the stuff all over. Even though this boat club offered to warranty the boat for 90 days I pretty much decided I dont want them working on my boat anymore so I said thank you and took it home. I already know and have on order a new 3 inch riser along with extra sets of gaskets to redo the new manifold and pull off the port side to inspect it.
Now, even tho Im running on borrowed time with that crappy 3 inch riser (why oh WHY would you replace the manifold and not the riser??) We took the boat out on the lake yesterday for a quick ride but could not get past 2300 RPM without backfire. At least I think its backfire as I never heard/been on a boat that did that before. Best I can describe is a loud POPing sound from the engine bay and seat of the pants feel like a loss of power for that fraction of a second. We turned around and put it back on the trailer. Got home and ran it under the hose and engine idles just fine. Only under load at about 2300 RPM out on the lake it was backfiring. Hey, at least the steering feels silky smooth now and pulling back upto the dock with one finger was a breeze
I did some Googling last night and this morning I checked a few things. I pulled the anti-siphon valve off the tank and it seemed fine. The little ball was clean and took very light pressure to push in. I tried to check the pick up strainer but it would not come out the tank. I lightly blew into the 90 degree fitting with my mouth to possibly clear off any gunk off the strainer and heard bubbling in the tank (I am not sure if this was a good idea or not to blow my hot breath into the tank but I figured a little wont harm much?) I checked and double checked the plug wires and cap and they all look good, but the plugs are on my list to replace soon. I went to local West Marine and picked up a new fuel/water separator filter and a bottle of Marine Sta-Bill and put about 10 oz into the tank. I poured the gas from the old filter into a glass jar but it seems like its ok, no water from what I can tell. I also used some CRC carb and choke cleaner all over and into the carb.
The engine continues to run fine at idle and up to about 1500 RPM but Im afraid to run any higher than that with no load in neutral. If I close the choke with my finger the engine dies right away (rules out a vacuum leak??) I also did another compression test and the numbers were the same as when I first got the boat home.. (around 175-180 all around)
I did not check the little filter INSIDE the carb. Could not really find it? Is it in the metal line?
Could ANYTHING with replacing the exhaust manifold cause this issue
Perhaps bad or now fouled gas? That first weekend we had it home I was not really thinking and just went to a local station to fill it up with gas. Im thinking maybe the old gas that sat there now mixed with new gas gummed something up?
Timing is always something people say to check but why would that have changed since last time?
I have not taken it back out on the water as it was getting late and other projects around the house took priority (I still stink of Florida irrigation gray water) but I may try and take her out tomorrow after work.
Any other things to check, think of? Again, could an improperly installed exhaust manifold cause backfire? Or just coincidence that this problem comes up now?
Thanks in advance.
Bought the boat from a "boat club" (this was not a club boat, just something the owner picked up to "flip"). The engine has about 350 hours on it so Im guessing it sat around quite a bit all those years. We test drove it on the water and I checked out as much as I could on my own and I took her home about 3 weeks ago. We took the boat out the first weekend and it ran great but noticed that the starboard side riser was running really hot and the steering was really stiff which I knew already but tried to lube it up with no luck. While I did have it out, it ran great. Got up to plane just fine and temp stayed about 168 or so. I brought it back and he agreed to replace the steering cable and manifold. Before I bought it he already replaced the riser/elbow so that was already new.
Two weeks later I go to pick it up and he along with his "tech" was still working on it. This is where it got interesting for me.
While he did replace the steering cable and got a new manifold, he did not bother to order a new 3 inch riser which even to my untrained eyes looked like crap. Full of rust and the mating surface between the exhaust and water passages were not smooth at all. He was also using some orange Permatex stuff all over everything! The manifold gasket and between the spacer and riser/elbow were oozing the stuff all over. Even though this boat club offered to warranty the boat for 90 days I pretty much decided I dont want them working on my boat anymore so I said thank you and took it home. I already know and have on order a new 3 inch riser along with extra sets of gaskets to redo the new manifold and pull off the port side to inspect it.
Now, even tho Im running on borrowed time with that crappy 3 inch riser (why oh WHY would you replace the manifold and not the riser??) We took the boat out on the lake yesterday for a quick ride but could not get past 2300 RPM without backfire. At least I think its backfire as I never heard/been on a boat that did that before. Best I can describe is a loud POPing sound from the engine bay and seat of the pants feel like a loss of power for that fraction of a second. We turned around and put it back on the trailer. Got home and ran it under the hose and engine idles just fine. Only under load at about 2300 RPM out on the lake it was backfiring. Hey, at least the steering feels silky smooth now and pulling back upto the dock with one finger was a breeze
I did some Googling last night and this morning I checked a few things. I pulled the anti-siphon valve off the tank and it seemed fine. The little ball was clean and took very light pressure to push in. I tried to check the pick up strainer but it would not come out the tank. I lightly blew into the 90 degree fitting with my mouth to possibly clear off any gunk off the strainer and heard bubbling in the tank (I am not sure if this was a good idea or not to blow my hot breath into the tank but I figured a little wont harm much?) I checked and double checked the plug wires and cap and they all look good, but the plugs are on my list to replace soon. I went to local West Marine and picked up a new fuel/water separator filter and a bottle of Marine Sta-Bill and put about 10 oz into the tank. I poured the gas from the old filter into a glass jar but it seems like its ok, no water from what I can tell. I also used some CRC carb and choke cleaner all over and into the carb.
The engine continues to run fine at idle and up to about 1500 RPM but Im afraid to run any higher than that with no load in neutral. If I close the choke with my finger the engine dies right away (rules out a vacuum leak??) I also did another compression test and the numbers were the same as when I first got the boat home.. (around 175-180 all around)
I did not check the little filter INSIDE the carb. Could not really find it? Is it in the metal line?
Could ANYTHING with replacing the exhaust manifold cause this issue
Perhaps bad or now fouled gas? That first weekend we had it home I was not really thinking and just went to a local station to fill it up with gas. Im thinking maybe the old gas that sat there now mixed with new gas gummed something up?
Timing is always something people say to check but why would that have changed since last time?
I have not taken it back out on the water as it was getting late and other projects around the house took priority (I still stink of Florida irrigation gray water) but I may try and take her out tomorrow after work.
Any other things to check, think of? Again, could an improperly installed exhaust manifold cause backfire? Or just coincidence that this problem comes up now?
Thanks in advance.