Had a bilge pump fail on me while I was washing down the boat after a long fishing trip. The back of the boat dipped enough to cause water to come back up through the exhaust riser and then cracked the head. I had water in only one cylinder (#6) as a result and we found which one it was by disconnecting the spark plug wire from the coil to the distributor. We then took one spark plug out at a time, cranked the motor over to see if water would shoot out, compression tested the cylinder, put that spark plug back in, and then went onto the next one. The crack was right in the water jacket next to the valve.
Replaced the head and all of the gaskets. Boat ran great for 2 weeks without many issues besides just some some minor electrical issues on the coil that was due to old connectors on the purple wires. The only thing that I did notice was that the WOT speed dropped from 29 to around 25-26 mph.
Last Saturday we had a 8 hour fishing tournament. Was cruising back to the harbor at 3500rmps and started to get some chatter in the motor and it went away if I decreased the rpms a bit. Didnt think anything of it and thought it was just the rockers that needed a readjustment. Then began to lose power and the speed dropped down to 15mph from 25mph. At that rate we werent going to make it to the cutoff for the tournament so I throttle back up and got it back up to 25mph but then the temp started to climb. I got up to 200 degrees but nothing over that. I limped it back into the harbor and then it wouldnt idle for more than 5 seconds. Of course I'm in a line of 30 boats to drop the cooler off for the weigh in. I had to blip it in gear and then throw it in neutral and rev it to 1000rpms to keep it running - that was not fun doing that 20 times. Limped it back to the slip and then started to investigate the issue tonight.
Pulled one plug at a time and did a compression test. Before the new head was swapped on - compression was 140 to 150 on all cylinders.
The head was replaced on the 2-4-6-8 side.
Plug #8 was not even hand tight and the electode was slightly melted. 4 was also loose and 6 wasnt much better. All 3 plugs had white soot on them from blowby and 4 was dark.
1-150
3-150
5-140
7-150
2 -150
4- 5
6 -120
8 - 0
So how bad do you think it is? What would have caused the plugs to work loose or were they not installed correctly? Could the lack of compression be just bad valves/rockers or do you think I actually melted the pistons?
Replaced the head and all of the gaskets. Boat ran great for 2 weeks without many issues besides just some some minor electrical issues on the coil that was due to old connectors on the purple wires. The only thing that I did notice was that the WOT speed dropped from 29 to around 25-26 mph.
Last Saturday we had a 8 hour fishing tournament. Was cruising back to the harbor at 3500rmps and started to get some chatter in the motor and it went away if I decreased the rpms a bit. Didnt think anything of it and thought it was just the rockers that needed a readjustment. Then began to lose power and the speed dropped down to 15mph from 25mph. At that rate we werent going to make it to the cutoff for the tournament so I throttle back up and got it back up to 25mph but then the temp started to climb. I got up to 200 degrees but nothing over that. I limped it back into the harbor and then it wouldnt idle for more than 5 seconds. Of course I'm in a line of 30 boats to drop the cooler off for the weigh in. I had to blip it in gear and then throw it in neutral and rev it to 1000rpms to keep it running - that was not fun doing that 20 times. Limped it back to the slip and then started to investigate the issue tonight.
Pulled one plug at a time and did a compression test. Before the new head was swapped on - compression was 140 to 150 on all cylinders.
The head was replaced on the 2-4-6-8 side.
Plug #8 was not even hand tight and the electode was slightly melted. 4 was also loose and 6 wasnt much better. All 3 plugs had white soot on them from blowby and 4 was dark.
1-150
3-150
5-140
7-150
2 -150
4- 5
6 -120
8 - 0
So how bad do you think it is? What would have caused the plugs to work loose or were they not installed correctly? Could the lack of compression be just bad valves/rockers or do you think I actually melted the pistons?